Here’s a list of stove part suppliers that I’ve used or know about. As I think on it, I may add more, so check back frequently. This list is current as of June 2019. These suppliers tend to come and go in many cases. If I’ve listed your outfit and you don’t want to be listed just let me know in an email. If you find a dead link or if you know of a link I should add, please let me know by emailing: firstname.lastname@example.org and I’ll try to add, update or remove it as required as soon as possible. Thanks!
I have this great old Primus 100 stove that I’m trying to fettle. I’ve got the NRV loosened up, but it seems to be stuck in the bottom of the pump tube and won’t drop out of the tube. It’s hung up somehow. It wiggles around and is loose down there at the bottom of the pump tube. I wonder if there’s some gunk in the tank that’s hanging it up?
What can I do to get it free?
Stuck and perplexed
a. there can be a little burr of brass where the vent hole in the side of the NRV barrel was punched in the barrel. You can use your alligator forceps gripping the NRV head with an unscrewing motion (like you are unthreading the NRV) to “unscrew” the burr past the opening in the pump tube end plate. Do it with the pump tube opening facing toward the floor to allow gravity to assist you. Use a little 400 grit wet dry sandpaper or a small file to remove the burr once you’ve got it out so it doesn’t give you problems again.
b. the other problem comes about from using lead NRV head washers. The lead will expand outward when the NRV head is tightened down, sometimes into the opening for the NRV head threads. This can hang up the NRV. Alligator forceps should help you to get it out, again with that unscrewing motion. Consider to switching to HDPE (#2 plastic) NRV head washers. You can punch them from the lids of food containers, so they are cheap to make and they almost never cause these hang-up problems. They last forever, too.
Here is an Optimus 111T that I “restored” for a client a few years ago. The client specifically requested the polished copper windshield and floor pan.
The embossed case was stripped, derusted, and repainted. The left hinge on the case was separated – the spot weld had failed. I silver brazed the hinge back in place before prepping and repainting.
Here are the beauty shots.
Sadly… the client was better at buying old stoves than actually operating them. Within three months of this restore the inept client had set the stove on fire, destroyed the paint, and melted part of the copper windshield surround. Sigh. :-(((
I often am asked to help out when a stove collector has problems removing a NRV (non-return valve) from the bottom of a stove’s pump tube. Usually the stove owner has done their best to remove the NRV, but has inadvertently rounded the soft brass head of the NRV valve. Sometimes I can get these damaged NRVs broken loose by using an “easy-out” (screw extractor bit) mounted in the end of a spade bit extension. I’ve actually made my extension a bit longer by welding an additional section of 1/4″ hex rod to the unit.
Sadly, this wasn’t possible on this old Monitor stove I was asked to repair.
I use the stove’s original pump lid, some washers, a bolt and a nut to make up this little pump pulling tool. It’s easy to do and works great without the fuss or expense of a “special” tool.
Usually I clamp the head of the bolt “tool” in my bench vise, hold the tank with one hand, and use the torch in the other hand to heat the area of the tank immediately around the pump tube. I put a wad of wet paper toweling all the way into the bottom of the pump tube to keep the heat from melting the solder holding the pump tube base block in place.
Here I’ve pulled the tube. But, I encountered some resistance as the tube would not completely exit the pump tube opening in the tank. It’s hanging up on the over-large pump tube base block.
It turns out that the folks that made Monitor stoves in England decided it was a “good” idea (not!) to make their pump tube end block larger in diameter than the outside diameter of the pump tube. There is no way to pull the tube while the end block is in place since its outer diameter is bigger than the hole the tube mounts in, so I had to desolder the pump tube end block from the pump tube and have it drop into the tank.
You can see in the photo above that that too-big end block is not going to fit out through that too-small hole. But, by using a small pair of Vise-Grip pliers to hold the end block, I was able to machine two facets into the block to reduce its diameter. I used a grinding wheel on a Dremel tool to do the work, taking off just enough to get the block out the opening. I also made sure I placed the facets in such a way that I could later clamp the block up in the three-jaw chuck of my mini-lathe to clean up the block.
Once the outer diameter of the end block is machined down in a couple of places, it pops right out. A little persuasion with some penetrant and some torch heat pops the NRV head loose from the block.
This stubborn NRV had a lead washer in place under the head. Didn’t seem to do much good to assist in removal, though. This is often the case with old lead washers as they seem to tend to get brittle and harder with age.
Because I had to desolder the end block inside the tank and with little control to the operation, the lead washer “migrated” a bit into the block and also into the threads of the block. I chose to clean the lead residues out of the block as I didn’t want this old lead to be causing me problems later on when resoldering the assembly together (I wanted to avoid contamination of the new solder with the lead). Spinning up the block on the lathe took care of the inside of the block and using a tap cleaned up the threads nicely without removing any brass. I’ve found through doing many pump tube pulls in the past that a 5/16″x36tpi tap is a remarkably close and completely functional match for the original proprietary non-standard NRV head threads.
So… I then soldered the end block back into the pump tube, then turned the pump tube end block flush with the pump tube diameter so that I could get the assembly (easily and sensibly) back inside the stove tank.
I needed to cut a special small pip for the small-size “tailed” Monitor pip cup.
I also chose to rebuild the head of the Monitor NRV since it was slightly different than a standard NRV in an effort to keep things sorta “original” looking.
First step was to machine off the twisted remnants of the NRV head.
Then I cut a socket or “mortise” into the head of the Monitor NRV head.
Next was to machine a small piece I could silver braze to the NRV head to restore the NRV head. I made a corresponding “tenon” to fit the “mortise” I’d cut in the original Monitor NRV head.
I cleaned up the brazed head, then hand-filed the two facets in the head.
Here is the completed restored pump tube and rebuilt NRV ready for reinstallation into the Monitor stove tank. Note my use of a shop-cut HDPE (high density polyethylene) plastic washer in lieu of a lead washer. I’ve found these HDPE washers to be entirely fuel resistant and superior to lead washers. The HDPE does not stick to the brass of the tube or creep into the threads of the pump tube end block. It also provides a fuel tight seal with much less torque required to make the seal than with lead washers.
Here I’ve used my simple bolt-and-washer tool to set up the pump tube in the tank for soldering, holding it in place with some stiff wire jigging. This jigging setup allows me to use both hands – one for using the torch and one for applying solder to the pump tube/tank joint.
I use standard electrical solder and rosin paste flux to do stove soldering. The rosin flux is inert until heated and any flux residues trapped inside the joint will not erode the brass of the tank on down the road. Acid fluxes will erode the brass over time which is why acid fluxes should never, ever be used around vintage brass stove work.
Inspecting the completed joint. I’m looking for any gaps or pits where solder may not have flowed into the joint. There should be a uniform silvery and liquid-looking seam of solder flowed in all round the joint.
The owner of this stove is a competent stove collector who may or may not chose to polish the stove. I’ll leave that chore to them. I hope this overlong treatise maybe helped some readers who were considering repairing their own stoves.
A Burmos 96 stove was sent to me for removal of a badly stuck NRV. After replacement of the NRV there was still leaking going on in the pump tube. I removed the pump while the stove was pressured and added some water in the pump tube. Using a small but strong flashlight, it could be seen there were several locations emitting streams of bubbles around the inside of the pump tube. This was likely caused by poorly drawn brass tubing that left stresses in the tubing back when the stove was made.
The pump tube was pulled and the tube was replaced with one I manufactured to match here in the BD Labs. Those photos follow.
“click” an image to enlarge
Here’s a quick post of a recent restoration of a Phoebus 625. This was one of a pair I bought on eBay as a two-stove Buy-It-Now package deal. Both stoves seemed mostly complete though this one of the pair was missing it’s spindle knob. And, of the two, this one came in a stuff sack while the other sported an actual tin.
Here are some shots of the process. click image to enlarge
The tank was stripped and glass bead blasted to provide a good surface for new paint. All the parts were degreased and cleaned. The pot supports were polished up on my buffing wheels. The tank was sprayed with VHT Engine Paint SP402 Burnt Copper. I like this color because it’s about the closest rattle can color to the original, plus it’s rated to 650 deg F (240 deg C) in heat resistance. Well-cured for three to four weeks, it’s pretty much proof to Coleman fuel.
The windshield was glass bead blasted and then painted with VHT “Flame Proof” SP998 Cast Iron. This is a paint rated even more heat resistant at 2000 deg F (1100 deg C). Unlike some of the other VHT Flame Proof paints, this one doesn’t seem to “brown” as much with exposure to direct flame. Good idea as the wind shield gets a lot of that from the preheat flames.
I added a brass preheat pan between the tank riser and the burner base so that the preheat alcohol will stay off the tank. Here’s how it turned out. click image to enlarge